杨平, 李波, 胡生双, 王文博. 2A12铝合金外套螺母裂纹分析[J]. 失效分析与预防, 2019, 14(4): 250-253. DOI: 10.3969/j.issn.1673-6214.2019.04.006
    引用本文: 杨平, 李波, 胡生双, 王文博. 2A12铝合金外套螺母裂纹分析[J]. 失效分析与预防, 2019, 14(4): 250-253. DOI: 10.3969/j.issn.1673-6214.2019.04.006
    YANG Ping, LI Bo, HU Sheng-shuang, WANG Wen-bo. Crack Analysis of Outer Nut of 2A12 Aluminum Alloy[J]. Failure Analysis and Prevention, 2019, 14(4): 250-253. DOI: 10.3969/j.issn.1673-6214.2019.04.006
    Citation: YANG Ping, LI Bo, HU Sheng-shuang, WANG Wen-bo. Crack Analysis of Outer Nut of 2A12 Aluminum Alloy[J]. Failure Analysis and Prevention, 2019, 14(4): 250-253. DOI: 10.3969/j.issn.1673-6214.2019.04.006

    2A12铝合金外套螺母裂纹分析

    Crack Analysis of Outer Nut of 2A12 Aluminum Alloy

    • 摘要: 飞机氧气导管2A12铝合金外套螺母在服役过程中出现裂纹。通过外观观察、断口宏/微观观察、金相组织检测、化学成分分析等方法,对外套螺母裂纹的产生环节和开裂原因进行分析。结果表明:外套螺母裂纹为应力腐蚀所致,裂纹呈分叉状,断口具有泥纹花样的腐蚀产物;应力腐蚀裂纹主要应力来源为外套螺母在装配连接过程中产生的周向应力;应力腐蚀裂纹源头主要出现在外套螺母的螺纹前几扣和端面部位;端面变形磨损或螺纹配合磨损引起局部膜层损伤和抗腐蚀能力下降,是导致该处成为应力腐蚀裂纹源头的主要原因。

       

      Abstract: 2A12 aluminum alloy outer nut for aircraft oxygen pipe cracked during service. The cracking time and cause of the nut were analyzed by means of appearance observation, macro/micro fracture observation, metallographic examination and chemical composition analysis. The results show that the cracking of the nut is stress corrosion cracking, with the characteristics of bifurcating cracks and mud pattern corrosion products. The circumferential stress due to assembly is the main stress for stress corrosion cracking. The stress corrosion crack initiated from the front several buckles of the thread and the end surface. Deformation and wear of the end surface or thread fit wear resulted in local film damage and decrease of corrosion resistance, so stress corrosion crack initiated from there.

       

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